cruisertoy
Explorer
Big thanks go out to Royal Rose from Wasatch Cruisers for comingto my rescue putting the 80 back together this weekend. I love
royal because he is so much more detail oriented than I am. He came over friday night and we installed the head, exhaust and lower intake. We were out there until 11:30 pm. Saturday morning we buttoned up the rest and got the motor running. It took me about 8 tries to get the distributor in the right alignment to finally time the thing correctly. (yes the jumper wire was installed on the firewall connector) After all was said and done I bet the first time we put the dizzy in it was fine and we just didn't wait long enough for fuel to fill the rail. I've only driven her a few miles today, but all seems to be running fine.
The only crazy thing that happened was tightening the head bolts. I've never done a head that didn't give you a final torq setting to hit. The 1fz has you torq to 29lbs then turn each bolt 90 degrees. Then turn each bolt another 90 degrees. We used the torq wrench for the 90's to get a feel for what the final torq was. Most of them ended up at 90+, but three of the bolt would hit around 70 and then not go any higher as then turned. These are torq to yield bolts and some things I've red say that is fine and other say that i should pull the three and replace them. I'll do a compression test sometime this week and make sure everything is tight. Cross your fingers.
The motor sure looks pretty with the shiny head, cleaned block and brand new hoses everywhere. I might just have to take a picture before I mess it all up again.
royal because he is so much more detail oriented than I am. He came over friday night and we installed the head, exhaust and lower intake. We were out there until 11:30 pm. Saturday morning we buttoned up the rest and got the motor running. It took me about 8 tries to get the distributor in the right alignment to finally time the thing correctly. (yes the jumper wire was installed on the firewall connector) After all was said and done I bet the first time we put the dizzy in it was fine and we just didn't wait long enough for fuel to fill the rail. I've only driven her a few miles today, but all seems to be running fine.
The only crazy thing that happened was tightening the head bolts. I've never done a head that didn't give you a final torq setting to hit. The 1fz has you torq to 29lbs then turn each bolt 90 degrees. Then turn each bolt another 90 degrees. We used the torq wrench for the 90's to get a feel for what the final torq was. Most of them ended up at 90+, but three of the bolt would hit around 70 and then not go any higher as then turned. These are torq to yield bolts and some things I've red say that is fine and other say that i should pull the three and replace them. I'll do a compression test sometime this week and make sure everything is tight. Cross your fingers.
The motor sure looks pretty with the shiny head, cleaned block and brand new hoses everywhere. I might just have to take a picture before I mess it all up again.