Here is the turbo out of the way:
See how the oil looks like it's being blown away from the turbo? It's everywhere. Hard to make a decision on where the leak is coming from.
I had a mess like that on mine. I finally found that the crossover rail line had a pin hole
in it (from rubbing on the head of a bolt or something) and it was misting.
After talking to the guys at NAVISTAR, I guess it it somewhat common,
and might be worth looking into here.
I replaced it with the HPX from Riff Raff Diesel.
Since it was already torn down, I also replaced the intake boots, added crush sleeves,
and eliminated the AIH for better air flow.
It's only time and $$, Right? lol
Nice. Pretty much the same stuff i did. You will love the results!
Here is the turbo out of the way:
See how the oil looks like it's being blown away from the turbo? It's everywhere. Hard to make a decision on where the leak is coming from.
So that curly thing in the intake y is the AIH? Was wondering when I had mine out
Yeah, all of that stuff, (including Bill Hewitt's Performance Mods) really woke mine up.
Glad it worked out fer ya! :victory:
How you like that whistle?
I highly recommend contacting Jodi for a custom tune. He seems to be the SHIZNIT on 7.3 tunes.
https://www.dp-tuner.com/contact-office.html
What tuner did you get?
He probably won't remember me, but tell him Eric sent you! lol
If you feel the need to roll coal, I'm sure he can accommodate that.
Eventually, I am going to take my rig to him, so he can do a "Live Tune", for optimum results.
Right now, it is probably producing more torque/power than I really need, so I will have him tweak it out.
Either way, it sounds like you are doing well on yours! Pics of gauge set up?