This weekend yielded some big results, even though it was a struggle the whole time!
Friday I set out to get the truck totally done, so I could start breaking in the gears on Saturday. I got up early to brave the DMV, and got myself a trip permit.
I started by getting shock mounts made. It turned out to be pretty damn time consuming and I had some struggles along the way, but I made it. The lowers are made from 1.5", .120" wall square tube. I boxed the frame in the top and made upper mounts out of flat bar.
The shocks are for a 2nd gen Tacoma, and have 10" of travel. I figured those would be pretty close in valving to be worth the gamble. I wish they were a little more vertical, but I also figured being a little relaxed of an angle might make them a little softer if they turned out to be too stiff.
I also whipped up a quickie tailpipe. My welder was fighting me, so it ate up time and made things look less sexy. Luckily it will probably never be seen.
My beautiful wife pitched in because she likes detailing interiors, and has quite the kit to do it right. The interior wasn't all that bad, but I noticed some mold starting to develop in a couple areas, and wanted a basic cleaning inside so I wasn't test driving it with the inside being nasty. She pulled the seats out, and the center console, and gave it a solid cleaning. She wants to take time to shampoo the seats and dive deeper, but I had to tell her to stop at sanitary haha. I didn't want everything wet for a test drive. My good buddy was over that evening too to hang out, and I (again) was behind, so he chipped in and helped her re-install the interior.
The interior on this is a solid 9.5/10, and I want to keep it nice. The rest of the truck needs a bath real bad, and the underside/under hood need a cleaning. But its at least presentable.
After finishing the shock mounts and exhaust, I really wanted to keep pushing. It was almost 10 at night, and I had a long day. I started to trim a fender, and decided to admit defeat, and clean up. There was a good thunderstorm forecasted for yesterday that is pretty uncommon for our area, so I cleaned the garage back out, and put the truck in the garage to finish.
Saturday morning it was sunny(the storm was coming in the afternoon), so I rolled the old girl out and got back to work. First thing I did was finish trimming the front fenders and core support.
With that done, I moved onto the bumper. My winch parts showed up this week, so I got those installed and checked to make sure it works. With a winch I'm more confident in, I set it in the bumper. The wiring for the turn signals was done real jenky by the previous owner(don't use scotch locks kids), so I cleaned that up. Then I had my wife help me lift the bumper on for the last time.
I tried to clean all the bubbling clear coat off the fairlead, but it was sort of pointless. I plan on going to a different setup. For now, until I order some goodies, this will work.
At this point, the weather was turning fast. The NWS alerts were coming in a lot over the radio for strong wind and damaging hail, so I put the truck back into the garage to finish up.
I moved onto marking and trimming the rear fenders. Talk about a mess!
Next was to bolt down the bed. It got loosened up when I had the frame pulled straight, thinking we needed to pull the bed. That ended up not needing to be done, so it was left loose.
Well, rust got the best of the bed bolts. Everything was tight as hell, even though they were half in. The thread size was not one I had a tap/die for, so I had to make a "chase tap" to chase the threaded holes on the forward 4 bolts. It was time consuming, but I didn't want to break a bolt in the bed and have that headache. I re-assembled everything with anti-seize to prevent it from happening again. The rear oddball bolts were easier to get to. 1 broke, but I just threw in a fresh one and a nut, and tightened the other side.
The part that bummed me most, is the plastic insert for the gas filler neck seems to be missing, so the damn door is duct taped shut hahah. I also see that we broke 3 of the 4 bolts off into the threaded holes on that. So I get to extract those later on. I'll also have to get that plastic part I lost so I can fill it up without holding the gun the whole time haha
Additionally, while working under the truck this weekend, I see the beginnings of some rust I want to nip in the bud before long. It's not that far along, but much more than I am comfortable with. So I will probably pull the bed down the road and treat everything and re-paint it all, as well as finish boxing in the frame.
With that pain in the ass done, I just had to bolt in shocks, pop the canopy off, clean the crap out of the bed, and she was ready for a drive! It was again, late at night.
I took a shower, and the misses and I went out on a drive to start breaking in the gears. Yukon has a pretty lengthy break in process, so we got 2 heat cycles done last night. It was a pretty awesome feeling to drive it again after almost 4 years!
This morning I took it out for a spin to complete 3 of 5 heat cycles, and filled the tank. I measured the ride height, and with a full tank of fuel, and some random dead weight in the bed, it still had a lot more rake than expected, so I dropped the shackles back down to the middle hole to lower the ass a bit. Even doing that, it still has a rake, which is good. I also adjusted the toe a little.
We drove it to my sisters for the afternoon and back to complete the last 2 cycles.
After putting about 115 miles onto it, I established that there are some kinks to iron out. Both T-cases leak out of the shifters. So I will have to sort that out. The ride isn't too terrible, but I was hoping it would have been softer. I do have a set of old man emu rear springs in my shed for this truck that I might try and swap in for the hell of it, but I'm not sure that will sort out the firm ride out back. It's most noticeable on harsh stuff like an unexpected pot hole.
The power steering seems to randomly whine, and after talking to some folks, I think I mounted the cooler a little too high. A buddy gave me a tip to bleed it better, and I will try that this weekend
There is something that seems to contact the frame or cross member under a heavy load, so I need to look into that. Then, there are just some rattles and squeaks that I will work on at some point. All in all, I am pretty happy with it. Even without a sway bar, it corners better than expected. Perhaps that's due to the stiff springs haha.
It was a pretty big checkpoint to hit, and I'm glad that despite struggling most of the way, I was able to still reach this point. There is still lots to do, but at least I can burn some miles on it and establish some confidence in it before driving it across the country this fall.
I'll be driving it to work all week, assuming it doesn't ******** the bed on me lol. More to come!