I guess I am not quite done completely refurbishing this truck. The axles I put in have been replaced, again. I had one OEM and one Cardone or something. The OEM was one of the ones I bought only a year or two ago but the outer CV boot clamp had been popped off during last year's Moab trip. I had a boot kit but since everything was fine I simply added some more grease to replace what was lost and put the new clamp on.
By the way, those cheap CV boot clamp pliers you can get everywhere? Absolutely worthless. The crimping "teeth" (for lack of a better term) bent and snapped when I tried to use mine for the very first time. Ended up using some end nippers I had.
So back to replacing the axles again. When I was under the truck early last week I noticed that grease was coming out of the CV I put the clamp on. Maybe I didn't get it tight enough? Or maybe there was a hole I didn't notice. The clamp seems to still be tight, I can't spin or move the boot at all. So maybe just a hole. At any rate, I didn't want to screw around with it so I ordered two more brand new OEM axles. I only was using the Cardone on the other side because that was the best axle I had laying around, but I don't really trust them, especially with the V8. Of course though of the two I bought one of them had a tear in the boot right off the bat from mishandling in storage. So back it went and a new one sent back out. Thank goodness for Amazon, they had the cheapest price on the axles (still a bit pricey at $230 a piece) and it was great not having to fuss too much with sending the damaged one back.
So that brings us to Saturday (yesterday as I am typing this at 12:30 AM Sunday).
Finally got a chance to finish cleaning the garage and pulled the truck in to work on swapping the axles. Hoo boy...
A few things popped up. First was I noticed my coolant level in the reservoir tank was a good 2 inches lower than it should have been (I had marked the level with a paint pen because I had some suspicions about the coolant level but it had sat at the mark for several months). Uh oh.
Checked around and sure enough I discovered coolant on the front crossmember. Thought maybe it was the pump, but that was bone dry. Couldn't see anything on the engine, so I looked at the radiator. Sure enough the top tank is starting to leak at the joint between the tank and the core. Great. Seeing how I had driven the truck for months after banging it around in Moab with no coolant loss, it's apparently just giving up on its own. Since I am going to be replacing the radiator now, I might go ahead and replace the hoses and pump as a precautionary measure. The hoses are looking a bit old and the pump, while fine, is not something I have replaced yet and I'd rather do it all at once than piecemeal it over time as things fail. We'll see how that goes. If I do that then I'm looking at around $650 for all the parts.
But wait, that's not all I get! While looking at the coolant on the crossmember I noticed that I was getting power steering fluid as well. Since I re-used the old hoses and replaced the o-rings with my best guess as to what sizes they were when I replaced the pump and rack, I figured I misjudged the oring for the high pressure line at the pump since that was the hose that was wet. But it wasn't wet at the fitting, just the hose. Apparently it was just as well that I had ordered new hoses (that way I could make sure I had something with the right o-rings) since the high pressure line was leaking at the factory crimp for the hard line to flex line joint. Seemed to be a weird place to leak, but oh well. But nothing is ever easy or simple. When I went to undo the fitting at the pump, I had a tough time trying to get it out. Not sure how, but apparently I over-torqued the fitting when I installed it so instead of getting the fitting on the hose to unscrew, it unscrewed the entire inlet fitting from the pump itself! Oh joy.
After a lot of research to make sure I had all the parts (there were three, the inlet fitting, the flow control body, and the spring for the flow control body) and trying to figure out how much it needed to be torqued (looked for quite a while and found no mention of the torque specs for re-assembling a Saginaw TC pump) I ended up doing a best guess and got it all put back together. Got the new hoses installed and ran the power steering fluid through a coffee filter a couple times before putting it back into the reservoir. I only bothered with doing that because the fluid I used was full synthetic that I paid far too much for to simply throw out after only month or so.
So once it was all back together and fluid back in, I started the truck up, let it idle for 30 seconds or so to let the power steering charge up, and tried to turn the wheel. Key work there, "tried." It would not budge. Not one bit. Crap...
Shut it off. Thought everything through, trying to see if I missed something or put the parts for the pump back in wrong or anything like that. Checked the fluid level again, saw it had gone down a little but not as much as I would have expected. Crap. More thinking. Ok, let's hope that it was because there was too much air in the pump and it wasn't getting any fluid past the flow control or something like that. Yeah, that's got to be it. Started the truck up again. That must have been it, because I was immediately able to turn the wheel just fine. Thank the Lord. Check fluid level again, it's below the dipstick which was what I was expecting to see the first time. Top it off. Call it good. Crisis averted.
Now onto the third thing I found, which fortunately was not as big of a deal as the other two. Ever since I dropped the front right corner off a ledge in Moab it seemed like I might have tweaked the frame or something because there was a noticeable slant to the nose of the truck in that direction. In addition my bumper on the passenger side looked like it had been pushed back and was also much closer to the grille than the driver side. Since I wanted to weight the truck without the bumper on anyway I took the opportunity to take the bumper off and inspect the frame to see what was wrong. Turns out it was not the frame (which is great news) but rather the body itself had crumpled a bit from getting slammed down so hard (primarily the core support which has the front body mount bracket attached to it). Fortunately fixing that was pretty simple, a big C-clamp and a 1/4" thick flat steel piece and a 1" thick aluminum block I had laying around. I was able to press the sheet metal between the two and flatting it back out so now it should site roughly where it was before. I am probably going to want to check the sheetmetal at the body mount on that side that is just aft of the front wheel well, I wouldn't be surprised if that suffered some damage as well. Now it is still possible the frame itself has been tweaked, but if it has it was not noticeable to me. I'll probably still take some measurements just to be sure. As for the bumper looking like it had been pushed back, I realized I am missing a clip for the grill on that side that would have sucked the grille back about a half inch, so there really isn't anything wrong with how the bumper is sitting, I just need to get a new clip, and I think I have some old ones kicking around somewhere as well.
So, yeah. Lots of "fun" trying to get this rig back to fully operational status so that I can finally start working on the rest of the modifications I want to get done before my Moab trip in April. Hopefully nothing else will come up before then, I'd rather be spending my time and money on the fun bits. But I'll hopefully soon have a rig that is in top shape and can be used for all kinds of fun.