I have a few truck updates and a tool one. In the process of picking up my car trailer from a coworker that was renting it from me I had my front drivers side brake line fail on me. It was pretty crazy as his driveway is about a 30* incline and I had to crank the wheel hard left and hold on the brakes pretty good to get the truck into position. As it was just about there the brake line cut loose and the truck started rolling forward in a hurry. Luckily I was able to jam the e-brake on after only 3' and no one was hurt at all! If the trailer had been hooked up I would have drug it behind me and possibly run my coworker over in the process. At this point I was already on the hook for picking up the VW that was about 60 miles south of my location so I had to make a quick trip to Napa and pick up a factory replacement line and a 6" piece of hard line to get the truck back on the road. It worked out pretty good and even though it looks like the hose is touching the spring it has a couple of inches of clearance lock to lock.
I plan on re-routing my main line back to the drivers side radius arm pivot and then to the axle where it will tee and use short flexible sections at the knuckles. That will eliminate the extreme stretch and possibility for getting caught up in moving bits.
I also replaced the drivers side door with a black one from Pull-a-part. I held off making the truck a multi color eyesore for a long time after getting t-boned, but with the window busted out and the door bent I had to something to get i back to being pleasant to drive. I might just paint it after I make the flat bed and ditch the red altogether. I don't mind it but my wife hates it!
I also spent some time getting the new garage up to snuff with a 220v outlet for the welders and a 20 amp 110v for grinders and air compressor. I needed to be able to fab at home so I am not spending so much time away from the fam staying late after work to make things. I also modified my engine stand to work as my mobile bender station. I wanted to be able to use the bender both vertical and horizontal so that added a little extra challenge to the project. I first found some tube that was pretty close to fit inside the benders rotating head and then cut a .5" slot in it 90* to allow the rotation from H to V but not beyond.
I used some .5" acme thread to pinch it tight on the inside and act as the stopper in the milled slot. It works decent but I think I will switch it to a QR lever that pulls a smaller section of pipe against the insider of the tube for more clamping force and less bending potential of the bolt. I love using random old parts from past cars on projects and it turns out the inner section of a Datsun 510 TC rod was a perfect handle for the acme thread!
I made a plate to mount the bender to with a slot in it so I can dial in the level of the tube before bending. I had to cut the pipe at a 45* to get the bender upright enough to zero out the tubing even with the built in adjustment
I added the necessary die holders that also serve as ballast
Here is the setup horizontal closed
Opened
Vertical
This should work pretty good and now that it is mobile it will allow me to be able to take it to other places and do some side jobs a little easier.