Well it was another back breaking weekend in the garage. Here's what was done and a few tips in case anyone else is looking to do this too:
- Pulled the struts out again for the millionth time...this time to machine the 1" spacers down to .75". While I liked the height but with weight in the back the front would sit higher worsening the positive camber and the CV angles. It's all about dialing it in...
- Replaced the inner tie-rods, one Moog and one AC Delco (since I'd purchased it as a spare a while back). This was probably the easiest compared to the rest of the tasks that got done this weekend. Just count the threads or measure the length to get the alignment close to the original; then I used a large vise-grip to loosen it at the steering rack end. Pipe wrench didn't fit.
- Replaced both lower ball joints in the front. Once the nut was off I had to use a two jaw puller to pop it loose (banging the knuckle with a 5lbs sledgehammer did nothing but left gouges in the knuckle). You also have to pull the CV shafts out to get the ball joint completely free- not enough clearance otherwise. However, since I had the strut out I only removed the C-clip at the wheel end of the CV shaft which allowed me to swing the whole hub up to free the ball joint. You'll need a lovely assistant or another pair of hands to do this.
- Lastly pulled the control arms out, which was easy enough but getting the bushings out was another story. The rear bushings are easy if you use a 2 jaw puller, see the pics. For the front bushings I tried the DIY method first since most folks don't have a shop press at home. The DIY method involves drilling the rubber part in a few areas, burning it out, slicing the outer metal sleeve very carefully so you don't cut the housing, then prying it or knocking it out. This was a long slow process (about an hour and a half) but ultimately worked on the first control arm. However, the second one just won't budge even with all the center rubber part completely hollowed out. At this point I had had enough and out came the shop press. It took a little figuring as far as the placement, the size of the die and other bits to use but 5mins and it was done! I used a 1-1/4" Craftsman socket as the press die which fit perfectly on the outer sleeve of the bushing and a couple of 1/2" extension. It took a LOT of force, the popping noise sounded like a gun shot, it was music to my ears at that point lol. Unfortunately I don't have the new bushings yet so the install will have to wait till next weekend or so. This whole project was quite involved or it certainly felt like it in 100deg weather and just about every trick tool out on the garage floor. Enjoy the pics
Look ma, no suspension:
Old vs. new
Easy peasy
DIY method...grab a drink or two it's going to be a while
Knock it out using the outside lip and it should come out like this...
If not, break out the big boys tools or bring it to a shop and have them press them out for $20