For some reason the ring that holds that drum in came off in August, it scored the drum pretty bad. The good thing about it is that I never knew, I just heard a weird noise for a little bit and soon after the noise went away, I just thought the tranny was hot and I kept driving it for a couple of months like that with no problems. So the drum and clip were wasted and this is the new replacement part from Ford. Nick found it along with the ground down C clip when he opened it up to convert the output shaft. I didn't have a choice in the matter, it is a $300 upgrade.. It could be in the newer transmissions already (mine is 2002 4R100)
So to bring the build up to date. I didn't realize that the metal shavings were floating throughout my trans and I didn't flush the lines before I put it all back together. $h@t for brains (Me thinks this is why the trans failed the second time) Nick found some ground up metal crushed between a clip and a bearing, which was making the awful squeal. Again I could have driven it another 2000 miles with no problem, it would have made noise , been a nuisance and would have eventually destroyed the bearing leaving me stranded somewhere. Thankfully he found the problem this time and hopefully everything goes back together today and I'll be back on the road, for good. Or at least until I get heavy pedal syndrome again and break something else.
When I get it home I'm going to trim the rear fenders so that the tires don't rub and probably install some air bags to help with the load, and ride height. Front bump stops are in order as well.